The numerical model simulation was applied in this research for 300 MW coal-fired power plant
combustion air system suction side. The purpose was power saving of station service in form of pressure
drop reduction. The numerical result of original system showed significant pressure drop regions which
were flow measurement instrument, 90o mitered elbow and inlet elbow respectively. After modification
each section, it was found that the maximum pressure drop decreased by replacing the flow instrument
measurement from orifice airfoil type to be average pitot tube 60 mm diameter because the original
installed obstacle at section area flow path up to 65%. The average pitot tube could reduce system
pressure drop 72% and save fans power about 42-54.5 kW. The results of modification both elbow by
fillet and installation guide vane did not have any significant effect with the overall pressure drop after
modify in CFD modeling.